A few posts back I was struggling with a weird lean condition in vacuum at 4500-5500 rpm. It looks like this:

In an effort to fix, I ended up replacing a number of parts.
Injector cleaning
I pulled the injectors and sent them off for cleaning. My thought was that it’s possible there were some chunks in the rail during install clogging up the injectors. Well they are fine. I labeled each injector then sent them to the injector shop in WA. He flow tested them and thought they were fine without cleaning.
Here’s the chart. They flow tested around 924 cc/min, which is less than the advertised 1050. He said that was normal, though, they look like all other ID1050s he’s tested. It seems his flow testing equipment is a little different than IDs. I had a set of EV14 550s tested by him and they tested low too

He refunded me a little and sent them back

Plugs / Coils
I didn’t take many pics, but I also replaced all plugs and all K coils with brand new stuff. The new coils don’t have the sticker on top

I also tested with the old foundry 3 harness, thinking maybe mine had a bad crimp or something

O2 sensors
I replaced both o2 sensors. I have AEM inline widebands. I bought them about a year apart, the sensors themselves looked pretty different, and one could have been further gone than the other.
LSU 4.9 sensors are Bosch part number 17025. I think there are a few other part numbers floating around where the variance is just wire length. I just got the 17025s. Rock auto had them cheapest at about $70 each


In the process of replacing them, i noticed that some of the wires were too close to the exhaust. One of the o2 sensors had a plastic collar on it that was sometimes touching the exhaust

The rear o2 sensor connector was too close to the exhaust, it got so hot the insulation of the exposed wire split

I clipped the tube back as far as I could, fixed the exposed bits with heat shrink, then covered all the wires with fire hose
A similar thing happened to the CAN side. Only the white wires split, whatever wire AEM used for white was lower temp than the others

I cut it way back, then totally rerouted that side.
Then more fire sleeve over everything, 1” fire sleeve over the o2 connectors, and more deliberate routing. Hopefully no more issues

I think we’re all up to date now. There’s one more big project to finish, then the car heads to the dyno end of June.

In an effort to fix, I ended up replacing a number of parts.
Injector cleaning
I pulled the injectors and sent them off for cleaning. My thought was that it’s possible there were some chunks in the rail during install clogging up the injectors. Well they are fine. I labeled each injector then sent them to the injector shop in WA. He flow tested them and thought they were fine without cleaning.
Here’s the chart. They flow tested around 924 cc/min, which is less than the advertised 1050. He said that was normal, though, they look like all other ID1050s he’s tested. It seems his flow testing equipment is a little different than IDs. I had a set of EV14 550s tested by him and they tested low too

He refunded me a little and sent them back

Plugs / Coils
I didn’t take many pics, but I also replaced all plugs and all K coils with brand new stuff. The new coils don’t have the sticker on top

I also tested with the old foundry 3 harness, thinking maybe mine had a bad crimp or something

O2 sensors
I replaced both o2 sensors. I have AEM inline widebands. I bought them about a year apart, the sensors themselves looked pretty different, and one could have been further gone than the other.
LSU 4.9 sensors are Bosch part number 17025. I think there are a few other part numbers floating around where the variance is just wire length. I just got the 17025s. Rock auto had them cheapest at about $70 each


In the process of replacing them, i noticed that some of the wires were too close to the exhaust. One of the o2 sensors had a plastic collar on it that was sometimes touching the exhaust

The rear o2 sensor connector was too close to the exhaust, it got so hot the insulation of the exposed wire split

I clipped the tube back as far as I could, fixed the exposed bits with heat shrink, then covered all the wires with fire hose
A similar thing happened to the CAN side. Only the white wires split, whatever wire AEM used for white was lower temp than the others

I cut it way back, then totally rerouted that side.
Then more fire sleeve over everything, 1” fire sleeve over the o2 connectors, and more deliberate routing. Hopefully no more issues

I think we’re all up to date now. There’s one more big project to finish, then the car heads to the dyno end of June.